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Brahma's update at 83K miles

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    Brahma's update at 83K miles

    My trials and tribulations without riding for three weeks now have me down in the dumps for sure. And, with having a spare bike, I should not have this worry. But that one too is hard down for the moment (2006 Stratoliner, 121K miles).
    Brahma needed new shoes, that's easy enough so I ordered a set. They came in but the shop could not get to swapping them for over a month. I thought to myself, "Self, you have R&R these wheels and have a different shop swap the rubber". I need to save some money anyway.
    Well, the dealer let me know 13K miles ago that when the time came to change the back tire, that the left TORS would not be able to go back on due to the significant amount of cancer on the 90* curve coming out of the crossover. So I ordered a full Viking exhaust system and have it standing by to go on. Sure enough, when I attempted to remove the left TORS, it literally feel apart.


    Next, I found I needed a 17mm hex head and a 24mm wrench to remove the wheel. Off to the parts store to get them. While out, at 6 different stores to include Harbor Freight, I could not find the 19mm hex to remove the front wheel. Not one single place had it. Amazon did so I waited a few days and it showed up.
    But back to the rear wheel; when it came off, I saw how horrible it looked with 83K miles of grime and oxidization, that should comes off. Here you can see the darkness that does not belong.



    I set up my saw horses and a couple of fence planks as a make shift work bench. I began cleaning with a heavy duty degreaser, holy cow this is a lot of work.
    I decided I needed to remove this gear piece and the brake disk for ease of cleaning. However, I got the gear piece off but not the disk.


    A day later, I decided that I had to remove that dang disk to clean this rim. I had already done to sand paper as the cleaner got the surface gunk off only to reveal a lot of corrosion.
    The disk is held in place by T40 Torx head screws that have been loctited same as the out gear bevel was. My screwdriver could not break them loose so off tot he part store to buy a 1/4 drive socket to use with bits. This off course is a small wrench and I needed a cheater to help apply my own torque to break the Torx loose.

    Finally, I have won a battle and showed I am stronger than an inanimate object. Unfortunately, it was the Torx bit...

    I had another bit and ended up getting all screws out without further drama.
    Then the disk refused to come off. I looked to see if something else was fastening it down and saw there was not. A rubber mallet loosen the aged grip enough for the disk to come free.

    Two days later, and I am still sanding the rim by hand. I know I must protect it somehow once I get it shined up. I decided that I will have the rim powder coated. I looked it up on line to see if there is a DYI method I could use when I discover that most shops bead blast the aluminum rims before coating. It takes a few minutes to prep this way. I have been sanding for days no and have a long way to go if I keep doing this by hand.

    Just working on the rear rim, I have yet to remove the front wheel. I will get to that today I hope and drop them off tomorrow for professional cleaning and coating.
    Last edited by Boog; 07-11-2021, 10:20 AM.

    #2
    Impressive. I bet you are sleeping good lol

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      #3
      Nice work but, you are changing that tire a little early, don't you think? I'm sure I see another 1/32nd of a mile in it!

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        #4
        That a lot of work but you'll have it looking good when you get done
        when you get done I'll bring my bike over and let u do the rims 🤣🤣🤣🤣

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          #5
          Amigo,
          I'm afraid you are reaping the results of Brama's outdoor living.
          I have found 0000 (4 ought) steel wool and any metal cleaner to work well for cleaning wheels.
          WD40 may also help break down the gunk.
          I surely do not envy you this job and wish you success!

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            #6
            I use a spark plug wrench turned backwards and an 18" pipe wrench to get the front wheel. It also works with a bolt that has a 17" head.

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              #7
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              Last edited by Boog; 07-17-2021, 07:18 PM.

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                #8
                Make sure you gently cut away the tape with a sharp knife.
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                Last edited by Boog; 07-17-2021, 07:20 PM.

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                  #9
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                  The bamboo rod didn't make it. Luckily I found a copper rod that would suffice.Click image for larger version  Name:	 Views:	0 Size:	300.9 KB ID:	15771
                  Last edited by Boog; 07-17-2021, 07:21 PM.

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                    #10
                    The first coat of shiny black is on.
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ID:	15774 First coat of shiny black is on.

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                    • barbagris
                      barbagris commented
                      Editing a comment
                      Bobby - When You've finished - I have a set of wheels that need doing.

                    #11
                    The trick with larger hex bolts is to get a bolt whose head fits into where the Allen key goes, then put 2 nuts on it and lock them together. Now you have an Allen key that you can use with a regular socket.

                    Comment


                    • barbagris
                      barbagris commented
                      Editing a comment
                      OR - weld the bugger into a cheap socket. FYI a 12mm socket and a 10.9 1/2" UNF bolt works well for option 1.

                      Or buy the right sized hex key - cheapskate. Or I'll tell Steinway!

                    • Boog
                      Boog commented
                      Editing a comment
                      barbagris, you say that as if I am capable of such advance mechcanics... ;-)

                    • barbagris
                      barbagris commented
                      Editing a comment
                      If welding concerns you - A 1/2" UNF bolt can be persuaded to sit tight in a 12mm socket by use of a large hammer.

                    #12
                    Originally posted by barbagris View Post
                    OR - weld the bugger into a cheap socket. FYI a 12mm socket and a 10.9 1/2" UNF bolt works well for option 1.

                    Or buy the right sized hex key - cheapskate. Or I'll tell Steinway!
                    There are three ways of doing things, the right way, the wrong way, and the Steinway.

                    or as Steinway & Sons prefer to say, there are three ways of doing things, the wrong way, the right way, and the Steinway.

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                      #13
                      Well, I am back at it again. New tire is installed and they coat of black. Then it got three coats of clear.

                      First to retape the fat tire
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                      The sun left thus auxiliary lighting was required.
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                      My makeshift jig.
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                      Before
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                      Final spray
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                        #14
                        I am curious about why you bothered to tape the throw away tire. I understand for the new one.

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                          #15
                          Steel I simply did it for practice.
                          Last edited by Boog; 07-23-2021, 08:29 PM.

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